Blasting of a 76cm diameter shaft was required to create an artificial entrance into Carroll Cave. A 6-hole and an 8-hole blast design were produced around an existing 23cm pilot hole. The burden was too large on the 6-hole design leading to poor pull and fragmentation (blockages of pilot hole). The 8 hole design caused too many shelves to be developed and poor pull because drill cuttings flushed into the drillholes before loading. An optimised design was developed using 6 holes being charged as two separate 3-hole blasts. This significantly increased pull to consistently over 80% and reduced the number of pilot hole blockages.

Figure 1 Burdens required for a burn cut (adapted from Langefors & Kihlstrom 1978)
The 6-hole design (Figure 2) provides the maximum allowable burden for the free face provided by the pilot hole. It has less drillholes, so less explosive is required and cycle times are reduced. As can be seen the calculated burdens (1.5 times the pilot hole diameter) are too small for the required shaft diameter, so the pattern is expanded to 76cm in diameter. This forces the burden into the ‘breakage’ region rather than the preferred ‘clean blasted’ region (Figure 1).

Figure 2 6-hole blast design
The 8-hole design lowers the burden and spacing, increasing fragmentation (Figure 3). It is blasted on two separate delays, reducing the likelihood of hangups in the pilot hole. The reduced burden and spacing also allows for inaccurate drilling.

Figure 3 8-hole blast design
Brazil tests were carried out to estimate the tensile strength of the rock. Tensile strength is the most important rock property with respect to blasting as rocks break under tension, not compression (Worsey 2001). Results were separated into 3 categories to show the heterogeneity of the rock mass.
1. Clean fracture in fresh rock - 12.7MPa
2. Clean fracture in perforated rock due to the leaching of carbonates - 8.55MPa
3. Fracture along existing discontinuities - 3.99MPa
The initial designs assumed that the natural scatter produced by a 6.4sec, #12 detonator would be sufficient to produce a millisecond delay. As all burdens were the same, the order of initiation was not considered important. This assumption was tested to determine its viability. Results showed a normal distribution with a much higher delay than anticipated of approximately 7.5s (mode – 7.48s, mean – 7.52s). This higher delay is thought to be due to excessive time spent in the magazines. The standard deviation of 89.8ms suggests the delays produced are sufficient for a successful blast.
The final tests to be carried out were vibration tests on some of the blast parameters that could be adjusted to improve the blast performance. These tests aimed to identify which parameters had the maximum impact on the reduction of ground vibrations, in order to optimise the blast design in a more efficient manner. The parameters tested included powder factor, stemming, decking, drillhole diameter, burden and spacing. Geophones were placed at 7.6m and 15.2m away from the blast to represent the nearest limestone structures to the pilot hole.
Results from the vibration tests (Table 1) show that the powder factor had the greatest influence on the production of ground vibrations. Increasing the powder factor by as little as 20% is seen to increase the ground vibrations as much as 150%. It should also be noted that introducing a cast booster as a primer also reduced the level of ground vibrations. Adjusting the stemming, burden and spacing also showed a considerable reduction in PPV. The only parameter that didn’t show a significant change in round vibrations was adjusting the hole diameter. A number of drillholes were set up using decks to lower the charge per delay. Though all decks had sufficient stemming according to the literature, all of the holes sympathetically detonated. It is suggested that the rules of thumb regarding the stemming length of decking drillholes breaks down as the drillhole diameter is reduced.
Table 1 Summary of vibration test results
| | 7.6m | 15.2m | |||
Blasthole | Powder Factor | PPV (mm/s) | % Change | PPV (mm/s) | % Change | |
1 | 3 water gel chubs | -11.18 | 46.67 | -15.24 | 150.00 | |
2 | 2.5 water gel chubs | -7.62 | 0.00 | -6.10 | 0.00 | |
3 | 2 water gel chubs | -5.59 | -26.67 | -6.10 | 0.00 | |
4 | 2 water gel chubs + 1 dynamite stick | -15.24 | 100.00 | -9.65 | 58.33 | |
5 | 2 water gel chubs + 1 cast booster | -5.08 | -33.33 | -4.57 | -25.00 | |
| | | | | ||
Blasthole | Stemming | PPV (mm/s) | % Change | PPV (mm/s) | % Change | |
2 | 33cm dirt | -11.18 | 0.00 | -6.10 | 0.00 | |
6 | 18cm dirt | -8.64 | -22.73 | -6.60 | 8.33 | |
7 | 33cm air | -12.70 | 13.64 | -9.65 | 58.33 | |
8 | 33cm water | -8.64 | -22.73 | -8.64 | 41.67 | |
9 | 33cm fine gravel | -8.13 | -27.27 | -7.62 | 25.00 | |
10 | 33cm coarse gravel | -8.64 | -22.73 | 8.13 | 33.33 | |
| | | | | | |
Drillhole | Hole Diameter | PPV (mm/s) | % Change | PPV (mm/s) | % Change | |
13 | 38.1mm | -3.05 | 0.00 | -4.57 | 0.00 | |
16 | 44.5mm | 3.56 | 16.67 | -4.57 | 0.00 | |
| | | | | | |
Drillhole | Burden | Spacing | Max | % Change | Max | % Change |
3 | 46cm | 61cm | -5.59 | 0.00 | -6.10 | 0.00 |
13 | 91cm | 122cm | -3.05 | -45.45 | -4.57 | -25.00 |
The optimisation process was carried out simultaneous with the excavation of the shaft on a trial and error basis. The individual variables were altered one at a time to assess their impact on the blast performance. There were two main problems with the blasting process, poor pull and blockages of the pilot hole. As the blasted material was being flushed into the cave through the pilot hole, blockages would stop the excavation process until the pilot hole could be unblocked. The main causes of blockages were too much material trying to flow through the pilot hole at once and poor fragmentation. Damage to the structures within the cave also had to be monitored.
There were a number of problems associated with the 6-hole design. Having all holes on the same delays saw too much material flow through the pilot hole simultaneously, creating blockages. Introducing separate delays eased the problem, however, the burden and spacing of the design was still too great to create sufficient fragmentation. This problem was exacerbated as the drillholes needed to be angled to keep a constant shaft diameter. Good pull could not be achieved because the burden at the toe was too great to fragment the rock (Figure 4).

Figure 4 Increased burden at toe results in poor pull
While the 8-hole design solved many of the problems associated with the 6-hole design, it introduced a series of new issues that had to be considered. The reduced burdens and spacings increased fragmentation, however, the addition holes increased the drilling time significantly, leading to two main problems. The additional drill cuttings tended to flush into the adjacent drillholes before loading of explosives. Pull was therefore unpredictable as the loaded length of each drillhole was different. This lead to many shelves being produced in the shaft as well as an uneven floor. By this time the shaft was well below the water table. The additional drilling time and abundant water reduced the driller's comfort, leading to inaccurate drilling, which affected the blast performance.
The optimised blast reverted back to a 6-hole design, however, it was drilled and charged as two separate 3-hole blasts. Because two blasts were required, any shelves produced by the first blast could be taken out with the second blast. The first 3-holes had a slightly smaller diameter to keep the burden below 1.5 times the pilot hole diameter to ensure sufficient fragmentation (Figure 5). It significantly increased pull to consistently over 80%, often gaining 100%. Though the two blasts increased the cycle time of the design, the additional gains in pull meant the advance rate was actually quicker than previous designs.

Figure 5 Optimised blast design
Drillholes for the final blasts were 107cm deep and 38mm in diameter. The three inner holes could be drilled vertically, which are more accurate than angled holes. Reduced drilling times improved the quality of drilling, further improving the accuracy of drilling. Each drillhole was charged with 4 sticks of extra-gelatin dynamite with shelves charged at one stick per 30cm. Drillholes were initiated with a separate LP delay to control the amount of fluid passing through pilot hole at any time. Drill cuttings were used for stemming, though groundwater was always present, increasing coupling.

Figure 6 Fragmentation of blasted rock using (a) 2 chubs of powersplit & (b) 2 1/2 chubs of powersplit
The would like to thank Paul Worsey, John Bowles and Soek Bin Lim of the University of Missouri-Rolla’s Rock Mechanics and Explosives Research Centre for their technical and practical assistance and the Carroll Cave Conservancy, especially Rick Hines, for their help and providing the project.
Hines, R. 2002, The Carroll Cave Digs [Online, accessed 10 June, 2002]. URL: http://www.cavediggers.com
Kirkbride, M., Worsey, P. & Rupert, G. 1995, Vibration Monitoring and Control of Blasting Associated with the Relocation of Highway H, Missouri Highway and Transportation Commission, Missouri, USA
Langefors, U. & Kihlstrom, B. 1978, The Modern Technique of Rock Blasting: Third Edition, Almqvist and Wiksell, Stockholm, Sweden.
Orndorff, Randall C., Weary, David J., & Sebela, Stanka 2002, Geologic Framework of the Ozarks of South-Central Missouri—Contributions to a Conceptual Model of Karst [Online, accessed 18 May, 2002]. URL: http://water.usgs.gov/ogw/karst/kigconference/rco_geologicozarks.htm
Weaver, H.D. 1980, Caves of the Gasconade (Ordovician); Carroll Cave [Online, accessed 20 May, 2002]. URL: http://www.carrollcave.org
Worsey, P.N. 2001, Blasting Design and Technology Lecture Series [CD-Rom], University of Missouri-Rolla, Rolla, USA.
[1] Student, School of Geosciences, Minerals and Civil Engineering, University of South Australia, Mawson Lakes Campus, Adelaide S.A. 5095, Australia