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T-Junction Dig 21
April 20 - 21, 2002

Disappointing

31.7 feet to Carroll Cave or 86.8 feet below surface 

Diggers: John Bowles, Greg Buckley, Bill Gee, Marty Griffin, Rick Hines, Ron Lather, Dave McCool, Jeff Page, Chris Wolters

We only got in one blast Saturday and pulled only a disappointing 1.2 feet.  Based on the weather forecast Saturday night we decided not to work Sunday.  We called John Bowles and he agreed to pick up the unused explosives Sunday morning.  Bill Gee and I spent the night at the schoolhouse, picked up around the dig Sunday and carried explosives down to the schoolhouse for John. 

Bill Gee camped at the schoolhouse Friday night.  He was unable to get to the dig because the ditch between the gate and the dig was a 40-foot wide roaring river.  By Saturday morning when Dave and Marty arrived with the explosive the water in the ditch was only about 2 feet deep and we were able to get across in Dave's truck.  The total rainfall for the weekend was 7.5" and most of that came down Friday night.

The steel plug was in the 9" pilot hole but was not holding water so it was easily removed.  The hole was nicely prepped and the template fit in easily.  A measurement found the hole clear to the cave but found the bottom of the dig at 85.6 feet below the surface (previously reported at 86.1 feet). 

Marty drilled 8 holes but was only able to drill one hole near the 9-inch hole due to a wide spot at the top of the pilot hole.  Chris Wolters had modified the template to move the center holes closer to the 9-inch hole to help insure that they blast to the bottom. 

Dave loaded 2.5 power split sausages into each hole.  Unfortunately I dropped the wooden rod, designed to press plastic stem plugs over the explosives, down into the cave.  Dave improvised with a fiberglass rod but this apparently pushed the plastic plugs in at an angle and in at least two cases cut the shock tube on the non el dets.  Dave knew he cut one tube when he was loading and loaded an additional sausage on top to try to detonate the charge below the plastic plug.  The tube he knew he cut was a white zero delay det.  After the blast Bill Gee carefully looked for undetonated explosives and founded 2.5 power splits and a yellow non el.  The one hole drilled near the pilot hole blew out near the full-drilled depth turning the pilot hole into an oval.  The rest of the surface required a lot of chipping to eek out the meager gain of 1.2 feet.  When we dig next we will have a large jackhammer to try to chip out the fractured rock a nd get a larger gain p
Terry DeFraties had provided a new 5-foot section of railroad rail for use in the 9-inch hole.  I cut two holes through the web of the rail and secured a heavy chain.  After the blast we found the chain hanging free with no rail.  When we pulled the chain out we found the loop end of the chain was still intact.  We must have blown the rail in two along the length of the web.

We well spend the next three weekends preparing for MVOR.  The next dig will be May 25-26, the weekend after MVOR.

There is still a lot of work to do at the MVOR site.  We will be working on the bonfire and other task each of the next three weekends.  Bring a chainsaw and a friend and come help.  Please contact Eddie or me to sign up.

Eddie      417-736 3195     caverebels@prodigy.net

Rick   913 897 4258    rickhines@aol.com   

See you at MVOR
Rick

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